Central Graben
14 April 2016

Appraisal well on the Jacqui oil and gas/condensate discovery, on a horst block previously tested by well 30/13-4. Jacqui Sandstone objective at 13,460 ft (13,308 ft TVDSS) was 582 ft deep to prognosis and below the GWC. Strong residual oil shows were seen but RCI showed water a gradient and two water samples were recovered. Thin (5 ft) oil sand was seen in Lower Jacqui. 30/13b-10Z was deviated up-dip and proved a 171 ft gross gas column in the Upper Jacqui sand to a GWC at 13,320 ft TVDSS.

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