Viking Graben
7 October 2020

Exploration well deviated NE to the Gair fault terrace, located down-dip of the Garten oil discovery, with a Middle Jurassic Beryl Formation main objective and planned TD of 14,000 ft TVDSS. Main hole drilled as pilot to 16,145 ft (13,392 ft TVDSS); over 600 ft high to prognosis and abandoned. Sidetrack deviated down-dip with TD of 16,875 ft (13,404 ft TVDSS) and also abandoned tight after 23 days.

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